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Texas
By
A.J. Foyt
The Indy car race at Texas Motor Speedway is second only to
the Indianapolis 500 because as everyone knows, to a Texan,
Texas is the best. I’m always very busy at that race because
I have a lot of friends and family who think like me. So the
pressure on my ABC Supply team to run well there is greater
than at the other races—with the exception of our sponsor’s
home race at Milwaukee, which didn’t go well at all this
year.
Looking for the best available driver, I asked my grandson
A.J. Foyt IV to drive the No.14 ABC Supply car at Texas
because he runs good at that high-speed 1.5-mile oval. He
hasn’t had the best luck there, and lately, neither have we
as a team but I was hoping to change that this weekend.
Well it didn’t happen.
On Thursday, we practiced at night and were pretty happy
with the No. 14 Honda-powered Dallara--we were in the top-10
when we quit running. A few guys popped in a quick lap right
at the end but we were satisfied that the car was running
good. It was the same in practice the next afternoon where
we ended up 12th but felt confident about qualifying.
When Anthony turned in a strong warm-up lap in qualifying, I
started thinking maybe even a top-6 run. Well it didn’t
happen. His four-lap average speed was slower! He ended up
22nd on the grid! In talking with the Honda engineers, they
felt we were geared too high. I agreed and we made the
changes for Saturday night’s race which started at 8:40pm
Texas (Central) Time...past my bedtime.
Anthony got a great start—he picked up six positions! Graham
Rahal’s accident on lap two eliminated him and two other
cars but Anthony was already ahead of them on lap one. The
more Anthony ran, the more his ABC Supply car’s handling
changed; it started “pushing” or flying the front end.
I had set the car up to push in the beginning but it pushed
a little too much and Anthony had to throttle her down which
he did. Because it wasn’t handling that well, he lost speed
and leader Ryan Briscoe was flying. Anthony pitted before he
was lapped but he’d lost so much track position while
fighting the push, that he lost a lap when he pitted. On the
first stop, we put in a turn of front wing to add downforce
to the front of the car. Anthony said that it helped but
after 20-30 laps the car started pushing again. We should
have added two turns.
When he made his next pit stop—again under green flag
conditions and again losing another lap to the leader—we put
in two more turns of front wing. Anthony said that made the
car a little loose at the beginning of the run but much
better throughout the run. That was obvious on the computer
because his lap times had really picked up. He came out of
the pits in 19th and worked his way into 15th by passing
cars on the track.
There was a caution flag for debris on lap 150 and when
Anthony pitted, the stop was quick enough (7.6 seconds) that
he went from 15th to 14th and we took out a half-turn of
front wing. Anthony was running with the lead pack at this
point because the ABC Supply car was handling well. In fact
he set his quickest lap of the race on lap 166. I started to
think we were going to get a good finish out of this race.
Well it didn't happen.
He was running 13th when the left front suspension broke
going into turn one on lap 172. The cameras didn’t catch it
until he slid across the track into the inside wall. We
didn’t know what happened so we kept watching the TV monitor
to see a replay which didn’t show how it started. We saw him
get out of the car which was a relief because the car didn’t
look too good on TV.
He said the left front went down, spun and slid backwards
into the outside wall and then came across the track and hit
the inside wall. It hit hard enough in the rear to break the
engine.
It could have been a lot worse and we’re all grateful that
Anthony got out with just a few cuts and bruises. It helps
that he’s in great shape and only 25 years old.
He was ok--except for the disappointment. Even though you
know it’s not your fault, you just feel bad. I felt bad for
him because he was running a good race—keeping it off the
wall when the car wasn’t running that good, and running
quick laps when we fixed the car’s handling.
The suspension failure was our fault, plain and simple. A
bolt broke on the pushrod. We are changing the procedures
for installation so it doesn’t happen again. To be honest,
it shouldn’t have happened in the first place. We had a
meeting that night and two team meetings on Monday. I felt a
change in attitude when I went to the shop today which I
take as a good sign.
So far it’s been a tough season for my ABC Supply team but
we are going to turn it around.
Starting now. |